Entries in Leadfoot (8)

Tuesday
Sep152015

Leadfoot: Them's the Brakes

Another of those everyday annoyances I just learned to deal with was the brakes. Some days were worse than others, but an imbalance in either the front or rear brakes meant there was a pulsation when applying the go-slower pedal that changed its frequency linearly relative to vehicle speed.

In my ignorance, I’d first thought it was the anti-lock brake system doing its on-off thing. So shoot me, it was seven years ago and I’d never had a car with ABS before.

But then the ABS light started coming on. It wasn’t always on, I just noticed it more during inclement weather, so in my ignorance (again), I assumed this meant the system was working extra-hard. No, I have no clue where I got this idea.

Later I learned that an ABS light means you don’t have ABS. I found this out after an event on the interstate forced me to use some heavy braking. I felt the rear of the car come loose and saw white tire smoke behind me. Once I’d gotten clear of the Darwin Award candidate who decided to cross three lanes to get away from an exit, I thought to myself, “The rear brakes must have locked up when the weight shifted forward. …But the brakes shouldn’t have locked up, because my ABS light is on, and that means the system’s work… oh.”

Supposedly, there’s a way to use the light to diagnose what the problem is, exactly. I was never able to figure out how to do that, but investigation found it to be a faulty wire from the combination of oil leaks and front-end collision I mentioned earlier. All of this meant the anti-lock brake system had nothing to do with the pulsation in braking power.

So it must be the brakes. I couldn’t feel the pulsation in the pedal, and the steering wheel didn’t pull, so it must be the one of the rear drums that’s out of round. Imagine you’ve put all your laundry in one side of your top-loading washing machine. Once it gets to the spin cycle, the machine is going to start doing the Jitterbug all around the laundry room. And that’s not going to be fun for anybody, because nobody knows how to do the Jitterbug anymore.

Because of the imbalance, passenger comfort requires effort on my part. Coming from highway speeds, a light touch of friction brings me down to where I can downshift into second. The brakes even out a bit and I can apply more pressure, but then I have to ease back off and modulate with the pulsation, lest my guest become an inadvertent head-bobber.

So the drums need replacing.

The parts are ordered and on the way when I find the HVAC fan only works on speeds three and four. The blower resistor has gone bad. As summer comes to a close, this is problematic. In the mid-Atlantic, summers get brutal with heat and humidity, and Eddie has zero tint on his windows. So from late May to early September, I’m quite content to leave the air conditioning on a higher speed. Keeps me cool, because the sun’s rays have little barrier to entry.

But as the Earth continues its orbit, we start to lose the heat, but keep the humidity until November. Now imagine that humidity combined with the greenhouse effect of a car with no tint. It all equals an uncomfortable drive for me (a man who prefers the cold) until I introduce the cooling and drying effects of air conditioning. And without the outside heat as a contributing factor, fan speed three is just too cold (even for me). But a bad blower resistor means that’s the lowest speed I’ve got.

The Internet is a great thing for what it can be. Yes, we use it to send pictures of our genitals to strangers who don’t want them, but beyond the dick pics, lunch tweets, and clickbait is an immense hoard of information that’s already indexed for immediate access. I typed into Google, “Pontiac Sunfire blower motor resistor,” and right below some shopping results were two tutorial videos on YouTube on how to replace the part. One of them even went so far as to advise on how best to orient yourself in the car when accessing the deepest recesses of the passenger footwell.

Was it difficult to get to? No. It was impossible. I had to remove the blower to make it difficult.

I was thankful for my cordless drill and U-joints. I’d managed to get one of the bolts out using my smallest of ratchets in this most claustrophobic of space, but the back-and-forth motion combined with the flexibility of the U-joint meant the socket kept coming off the bolt head. Relief came from the constant rotational force of the electric motor in my lime-green drill.

And while the blower was out, I cleaned out the dead leaves. Now, with the new resistor and a clean blower I’ve got all my fan speeds and they work better than they did before they stopped working.

This I did while laying upside-down on the reclined passenger seat, my feet right about where a rear passenger’s ears would be. Actually, someone sitting there would have been helpful, so I wouldn’t have to fumble blindly for the right socket extension from the half-dozen I’d stowed in the cup holder.

Back down at my parents’ house with brake parts from the Internet, I pulled the rear wheels and hammered off the brake drums.

I’ve never been a fan of drum brakes. So many different parts, all needing to work together to achieve the same result as squeezing two pads on a disc brake. Every time I’ve had to replace something, I take a dozen pictures with my phone to reference how everything goes back together. And I always miss something in the pictures, so I’m at a loss with that one bit during reassembly, leaving me stabbing at straws until the springs are able to hold everything together tight enough to fit the drums back on.

About the time I’m about to clamp the new shoes in, Dad comes out and notices a leak in the brake cylinder.

That’s bad. Like, “need to replace it now before the problem’s even bigger” bad. YouTube showed me how bad it could possibly be when I’d asked the Clarksonion Rhetorical.

YouTube was also helpful when it came to removing the cylinder. The brake cylinder on a GM J-Body is one of those parts that’s put on before attaching the wheel hub. This makes it difficult to remove almost on the same level as the blower resistor. Thankfully, there’s a nice Canadian fellow with a liking for lock pliers who will show you how to remove it with a lot of hammering and a long screwdriver.

Once again, Eddie shows up in the neighborhood, here comes the sound of hammering steel.

Dear General Motors: In my experience, a wheel cylinder is more likely to need replacing than the wheel hub. Why would you not make the former easier to remove without first taking off the latter?

Their answer, apparently, is to equip the wheel hub with a hole on one side. This (theoretically) allows enough room to rotate the cylinder until it can be maneuvered free of its prison. But even with this “room,” it still took considerable hammering and prying to liberate the leaky little bastard.

And it took even more hammering and wedging to shoehorn in its replacement. This is all while brake fluid is dripping into an ever-expanding puddle. And the fluid is such a lovely shade of ink-black. That’s because I’ve never flushed the brake system. I need to do that soon as I get the appropriately-sized plastic tubing. There’s a plan in my head for that.

And after that headache, putting the new shoes on was the part I’d been dreading. Imagine a jigsaw puzzle, but none of the pieces fit until you put it all together. Then the shoes need extra hammering to get into place because the holding springs won’t do that job by themselves. Even when all the pieces are in place, the shoes kind of float around, contained only by the drum, so they need tapping into place so the drum can fit around them and line up with the wheel studs.

With the wheels back together, I rolled Eddie’s front wheels up onto ramps to drop the transmission pan again to replace the filter I should have replaced before. That went well.

Not so much trying to replace the spark plugs. The number four plug is possibly cross-threaded.

And I admitted defeat with trying to replace the alternator, which feels ready for retirement. But while I was able to pop the end of a serpentine belt remover into the appropriate 3/8” socket built into the tensioner, the arrangement of the engine bay was such that I didn’t have enough room to sufficiently loosen the belt. I could have gotten creative, but the day was long enough and I put it, too, aside.

So at the end of it all I’ve got a less-effective handbrake and the pulsation can now be felt more in the pedal than the body of the car. So I accomplished nothing I set out to do and only succeeded in preventing a bigger problem.

Not my most productive day. But the Eddie runs enough to trek 400 miles each way for my vacation. I’ll just keep my tools in the trunk when I head out.

Wednesday
Aug262015

Leadfoot Video: Rods and Cogs

A car’s fluids are all different colors so you know which is which without having to run a chemical analysis. I’m sure they all taste differently too, but I don’t recommend preparing a cheese platter to pair with them at your next social gathering.

But why does transmission fluid have to be red?

After seeing a puddle of it magically appear under my car after work, I’m convinced its visual similarity to blood is intended to strike fear into the heart of the automotive owner. Seeing a spill of gearbox oil evoked the thought of a loved one bleeding out on the duvet.

That’s not quite the thought that came to my mind, but that’s because I have no idea what a duvet is. But I did want to grab a handful of towels to stem the bleeding. But towels would only go so far. Eddie needed surgery and a transfusion.

The puddle of red drippings was really just the last nail in the “I have to do something about this” coffin. At times, Eddie’s transmission would slip, but only in the right conditions. Leaving the gear select in automatic, and turning left onto my home street, applying some throttle persuasion to carry on through the off-camber turn, the engine would rev up as if it were in neutral. After reaching about 3500rpm without actually going any faster than before, the computer would decide “Time for second gear,” and engage it. The gears would suddenly catch, engine speed is back down to about 1200, and I’m instinctively taking my foot off the Go pedal because I’ve just received a kick in the backside.

This was due to low transmission fluid. An automatic gearbox is a bit like me: it doesn’t work properly if it hasn’t got enough fluid. The difference between the two of us is that while the transmission needs Dexron, I’m much less picky. I can run on water, orange juice, Coke Zero beer, rum, whiskey, regular unleaded or the blood of my enemies. Always with ice, of course.

Adding fluid mitigated the issue, but when that problem returned, I knew I had a leak somewhere. I just had no idea how bad a leak it was until I’d stopped the oil leaks. Then, the slipping got so bad I added another quart of Dexron, only to find those frightening red puddles the next day. I knew then that a bottle of stop-slip wasn’t going to do the job, so it was back to that online retailer of auto parts. And because I had a coupon, I figured, “Why not do the tie rods, too?”

Tie rods are another of those parts that just wear out with age. They’re a critical part of steering the wheels. By that, I mean they actually turn the front wheels so the vehicle may proceed in the desired direction. If an end breaks… well, best case scenario is the car stops moving. Worst case is the car starts going in an undesired direction.

So after 15 years, I’m wagering Eddie could use some new ones. I don’t want him going in undesired directions.

And the last plan on my mind is replacing the output shaft seals. These are designed to keep the transmission fluid inside the gearbox while still allowing the axle to spin freely. My research found them to be a likely leak candidate. The parts being only $5, I figured it couldn’t hurt.

So, with a few cans of brake cleaner, Scotch-brite pads, disposable nitrile gloves, *all* the tools I own, and the parts I’d ordered, I made my way back to my parents’ house. I also brought a six pack for my dad as payment for borrowing his grease gun.

The day started off rough. After loosening the axle nut (and having to buy a deep well 30mm socket), standing the car on a few four-by-four wood blocks and taking off the wheel, I hit my first snag.

Contrary to the norm, the stock tie rod ends aren’t secured with a castle nut and cotter pin. For the uninitiated, here’s a picture of the standard setup. The pin runs directly through the bolt and the open spaces in the nut to keep the assembly from unraveling.

Instead, Eddie’s tie rods were secured with some kind of epoxy inside the nut, and no amount of penetrating oil would facilitate its release; only leverage would do. I didn’t discover this until after having to borrow a deeper 18mm socket than the one I had. Because I didn’t have an 18mm open-ended wrench.

Hey, I never said I’d had every tool I’d need.

So then came removing the tie rod from the knuckle. Funny, everyone online made it look so easy. One guy made it happen with a few taps of a hammer. So in my arrogance, I thought I could make it happen with less effort.

I’m starting to think my parents’ neighbors have begun to associate Eddie’s appearance with the sound of hammering on metal, because no one batted an eye as I wailed on this God-forsaken steering rack extension.

WD-40 wasn’t doing me many favors that day. When the tie rod wasn’t going anywhere, I cut out part of the already-punctured boot in the aim of applying oil from above and letting gravity help with the capillary effect.

While (I hoped) the oil did its work, I turned my attention to removing the axle in order to replace the output shaft seals. Two bolts keep the spindle firmly connected to the strut. They’ve got teeth around the shaft nearer the head, to keep them from spinning while tightening or loosening their corresponding nuts. The friction these teeth provide also make them difficult to remove without the use of a hammer.

But these strut bolts weren’t nearly so stubborn as the tie rod end, so a few good whacks and they popped right out. There was still some residual friction between the spindle and the strut, so it took a bit of leverage to pry it free, but free it was. Some taps on the outside of the wheel axle had it loosened from the hub as well.

But being free of the strut wasn’t enough space to wiggle the CV joint out of the hub completely. The spindle needed a bit more freedom, and since I was already taking off the tie rod…

Nope, still seized.

A visit to the auto parts store later via my sister’s Golf, I had in my possession a borrowed tie rod end separator. That, along with the hammer used liberally earlier, finally made short work of the seized connection. What a satisfying “thunk” that was.

The outer end was indeed shot. No resistance in the joint, contributing to the loose feeling in the steering wheel. The inner joint was stiffer, but not by much.

Next was dropping the tie rod back into the spindle for added leverage so I could undo the lock nut.

Yeah, turns out the outer end wasn’t the only thing that was seized. And all the WD-40 in the world wasn’t about to undo fifteen years of elemental exposure without the assistance of some serious leverage.

Enter, again, the come-along. Yeah, seems like I can’t ever stop keeping that thing in Eddie’s trunk.

Wrapping mule tape around the maple tree in front of the house and clamping some lock pliers onto the nut, the come-along was hooked up in between.

It’s after snugging up the ratchet do I realize the only thing holding up the front of the car is a couple of four-by-fours. No, I’ve decided I’m not stopping.

Turns out an emergency brake is more than enough to keep Eddie from moving before the outer tie rod breaks free from the inner. Thanks, Physics!

With that loose, I counted the number of turns it took to get the outer end off and turned my attention to the still-seized nut.

At least, I should have. I should have taken a bucket of WD-40 and dipped the tie rod into the immersion for several hours. But I didn’t. Instead, I was so aggravated by the tie rod ordeal that I started on the transmission pan.

For all the research on the matter I conducted, I really should have discovered that there isn’t a drain plug for the transmission pan. Instead, armed with the assurance that “the fluid will come out somehow,” I started work. So I shouldn’t have been surprised when the super-simple catch can (consisting of a piece of molded plastic which feeds into used 2-liter soda bottles) would prove insufficiently small for the amount of drippage that would take place.

So a mess was made. There’s probably still an oil stain where all that oil dripped onto the asphalt.

See, when I saw there wasn’t a drain plug, I thought I could contain the flow by positioning the narrower end downhill, and jacking the opposite side slightly higher. In my mind, that would minimize the spill if I undid the downhill bolts first.

Perhaps it did. Perhaps the smallest mess possible was the one I’d made. It’s still a lot of oil spilling everywhere, because I’d forgotten that when oil can potentially go somewhere, it will.

Regardless, I upgraded to a bigger catch can. When I say “bigger catch can,” though, I mean a two-foot diameter, two-inch high circular pan, the true purpose of which I could not imagine.

So, slowly opening the uphill bolts on the pan, I eventually got the spillage to the point it was all pouring into the pan. That made me happy.

Eventually, the dripping stopped, and I could completely remove the pan without gearbox oil splashing everywhere.

Free of the anxiety over unpredictable drippings, I could finally examine the problematic gasket. Being so non-uniform in its structure, I’m left to assume (post-operation) it’s a liquid gasket. That’s to say whoever applied it squirted silicone onto the mating surface, then squished the pan into place and tightened the bolts, but not too much.

This must be why the pan is leaking again. All the bolts I tested were loose. Clearly, the plan was to bring me back to the shop soon for more maintenance.

Thinking back, I remember a trip to Jiffy Lube while I was still in film school. The kindly manager told me I had a transmission leak. Those words scared me as much then as they do now, because I was about to embark on a project that would have me commuting 100 miles round trip each day for two weeks. If not for the voyage upon which I was about to embark (the next day), I would have waited for dear ole’ Dad to give me a second opinion. Instead, I saw the distance I must travel with this potential problem lurking, and ended up dropping $300 on what was initially a simple oil change. I now see that Jiffy Lube simply used liquid silicone to make a new gasket instead of calling around to local shops to see if anyone had a proper gasket for the 3-speed.

Five years later, I’m left with red puddles. The oil leaks might have contributed to the degradation, but I’m comfortable blaming the shop.

Scotch-brite, brake cleaner and elbow grease had the mating surfaces clean and ready for the new gasket. The bolts also got a cleaning, because liquid gaskets can and will go everywhere. I’d also cleaned the outside of the filter, since it had fallen out of its mount when I was wrestling with the axle.

Which wouldn’t come out. Of course, the filter fell out on its own, but the axle is stuck in the output shaft. Granted, I didn’t have any tool that would have properly facilitated the axle’s removal. I suppose I was under the impression that an axle could be removed with confidence and a stern talking-to. But no.

Stuffing the axle back into the wheel bearing, I turned back to the tie rod. Yeah, that tie rod, the one that I didn’t dip in penetrating oil like I should have. That lock nut is so seized that trying to loosen it with the come-along just turned the inner tie rod itself. It was enough to get the outer one off, but because I couldn’t get that nut free, I couldn’t take off the inner boot, which is what stops me from applying the special inner tie rod remover tool. Daylight was burning, and the inner rod felt okay enough for me to put it on the back burner. For now.

With the lessons learned from the driver’s side, I attacked the passenger side. Made for about the same progress. And the same lack of progress.

The sun was about to start hiding behind the houses, so I screwed on the new outer tie rods, dropped them into the spindle and applied the castle nut and cotter pin. None of that epoxy-in-the-nut nonsense.

I then returned to the transmission pan. Had I used ramps to get Eddie in the air, I would have had more space to work with, but the floor jack I have is really only meant to get the car high enough to extend the suspension so the wheels can come off. It doesn’t allow much space for crawling around underneath. I also had to somehow keep the gasket lined up while positioning the pan for attachment.

Enter duct tape. Duct tape was my friend in that moment.

No, I hadn’t taped the gasket to the pan. That would have been stupid. Instead, I slotted some bolts into the holes and taped the heads to the pan. Those bolts kept the gasket in place while I held the pan against the housing and fumbled blindly for another bolt to thread by hand just barely outside my reach because I don’t fit under the car unless I’m flat on my back.

At this point, the cordless drill I bought is earning its keep. A 3/8” socket driver meant I wasn’t spending my time down there with a ratchet. Instead, it was setting the drill’s clutch and pulling the trigger until the thing stopped spinning.

The day’s charms were wearing thin on me, so I expedited putting Eddie back together and cleaning up the spilt oil with the grease-fighting power of Dawn and a hose. Worked better than I thought it would.

Driving Eddie to test, I knew right away he’d need an alignment done. The steering felt tighter, but tire noise was intrusive even at ten miles per hour. Also, while steering straight was fine, when turning right the car wanted to steer back to center. And turning left made the car want to turn left even more. Toe adjustment was definitely in need.

What I hadn’t noticed when driving to the shop was that Eddie wasn’t using all the available gears. That’s because I didn’t drive anything resembling fast when he was out of alignment. No, it wasn’t until I got onto an interstate after having the alignment done did I ask myself, “Shouldn’t it be in third by now?”

In a three-speed gearbox, third gear is kind of important. At highway speed, second gear has the engine turning around 4000rpm. That’s the peak of the torque curve, so it’s very sprightly and easy to overtake the left lane hog in a Camry.

Why is it always a Camry?

And the engine sound great at four grand. As long as it’s under load. Otherwise it’s just a loud drone, like a vocally-amplified economics professor.

Despite that, the steering feels good. Like I’m driving a car that’s eight years old instead of sixteen. I doubt I’ll ever get Eddie back to showroom condition without some real investment on my part, but I can do my best, can’t I?

Chatting with my car guy coworker, he suggested a bit of the gasket might have been sucked up into the transmission and was blocking a valve, preventing third gear from engaging.

I let it go, because I was tired. Also, my commute to work never has me exceeding 50mph, so the car is comfortable with second gear at that speed. Feels like I’m on a track day, only on my way to work.

I was prepared to let it go until I could get time to replace the transmission filter. Then, after a busy night at work, I was headed home and, upon joining Route 50, I noticed the engine wasn’t turning nearly so fast as before.

Third gear came back. All by itself. I’m now convinced this car is magical.

I’m still going to replace the filter, because I’ve no idea when it was last done. And yeah, I cleaned it, but it’s still something that I should have thought of replacing when I cracked open the pan in the first place, but I can only think ahead so many steps.

Also, that ABS light came back on…

Thursday
Nov132014

Leadfoot Video: Rockin' Dat Bass

Cars last a long time these days.  Sometimes that’s a not-so-good thing.

Don’t get me wrong: there are great benefits to your car lasting to the end of days.  The average price of a new car has never been higher, so it’s nice that your investment goes a long way.  Plus, the used-car market would suffer greatly if an Accord (or my old Caravan) didn’t last 200,000 miles.

But technology moves faster than it takes a Yugo’s bumper to start rusting.  In the time it takes you to pair your phone’s Bluetooth, this year’s Lexus can become last year’s Oldsmobile.  Luckily, when you realize CDs are the new mini cassette, there’s an ample aftermarket that will let you swap out your factory radio for something with this season’s bells and whistles.

That’s exactly the recourse my mom took when the CD changer in her 2003 Voyager kicked the bucket.  And because I’m cheaper than those guys from Best Buy who drive Beetles, I’m the one she asked to install it.

I sent her to Crutchfield, since they include the extra stuff necessary for to install an aftermarket head unit into your particular make and model, including antenna adapter, wiring harness, and mounting frame.  I didn’t want to be stuck without parts.

It was also almost time for me to replace the torque strut in my Sunfire.  Last time, I’d resolved to buy a performance part with polyurethane bushings, instead of one with OEM-spec rubber.  The engine’s age has led to multiple oil leaks, and oil eats rubber.  But it apparently doesn’t eat polyurethane.  So I bought a $50 part to replace a $20 part in the hopes of never having to replace it again.  Odds are, it’ll outlast the car, depending on whether I come into some money and can afford to rebuild the engine.

So I made a day of it, starting with the radio.

Step one in any process involving electrically-driven components is to disconnect the battery.  It’s less of a concern over electrocuting yourself than it is creating a short, damaging the battery and possibly other things.  A high-school teacher of mine told me he once saw a car engine melt from a short circuit, caused by an improperly-installed stereo.  (That one involved running a wire through the firewall without proper insulation.)  All things considered, electricity is one of those invisible things that can kill you, so I disconnected the battery.

This Voyager is from the Daimler days of Chrysler.  The buyout was supposed to be a merger of equals, but the only thing worthwhile that Chrysler got was the LX platform, upon which the Charger and the 300 were built.  They also got the Crossfire, based on the old Mercedes SLK, but all of them were built with cheap materials and suffered poor quality.  (The worst thing Daimler did, in my opinion, was to kill the ME Four-Twelve; a turbocharged V12 supercar built by Chrysler engineers with Mercedes parts that was designed and built in just eighteen months.  But it out-performed the $500,000 Mercedes SLR, and Daimler couldn’t have that.)

So the Voyager has cheap materials and build quality.  It was designed to be assembled in a hurry, to maximize productivity.  So the center console is held on by six metal clips and two screws, obscured by a small pop-off panel.  Screws are easy.  Invisible metal clips that need to be pried off always make me think I’m going to break something.  Proceed cautiously.

The panel does eventually come off, after come cringe-inducing creaks.  It’s only necessary to remove the top-most wire connection (the one for the hazard light toggle and rear window wiper controls) to get the panel out of the way, but you could remove all three of them by sliding the red latches out and the connectors will come free.

Then comes the removal of the old unit.  It’s held in place by four screws, easily removed.  I was a bit worried that Daimler might have gone with some weird fastener head, like a pentalobe, in order to make sure their own mechanics are the only ones who could service their products, like Nintendo and the tri-wing bit.  But rest-assured, Daimler decided a Phillips head was cheaper in the long-run.

If ever you needed a reminder this is from the Daimler days, it’s printed on top of the head unit.  A more subtle clue in in the snap-lock antenna connection.  The connection releases by pulling the black collar away from the stereo unit, but only in just the right way.  Seems to be on a time-delay of some sort, because it took me and my dad some fifteen minutes of pulling and pushing and prying and prodding the connector every which-way before it finally relented.  The speaker wire harness is much simpler, I thank whatever higher power.  A simple clip-lock connection held that in place.  The connector for the CD changer was an aftermarket installation, and rather than pull the cable all the way through the dash and passenger-side door sill, I just tucked it deep into the dash.  There’s plenty of room in there, after all.

The mounting bracket Crutchfield sends installs into the dash using the four screws that held the original radio.  I am a bit worried about the style of screw they used, which looks more at-home fastening pieces of wood, as it seems to drive into some kind of metal clasp.  But I suppose it is hard to fit a nut, washer and bolt into such a confined space on an assembly line.  So here we are.  The DIN sleeve, which holds the actual head unit, slides into the bracket, and you bend down the appropriate tabs (determined by sight) to keep the sleeve securely in place.  Tabs further out from the center correspond to a thinner bracket.  If it’s still wiggling in the frame, use a tab further-out.

So now comes connecting the wiring harness.  Do yourself a favor and buy an actual wire stripper/crimper.  The harness from Crutchfield was pre-stripped (nice touch), but the length was excessive for the connectors I had.  I had a wire cutter/stripper, but it was a cheap one, and didn’t crimp so well, so it only served to trim stripped wire and strip wires on the harness from the new head unit’s manufacturer.  Dad had a real crimper, made the job easier on the crimping end.

Now, this is not the first time I’ve installed a head unit.  The first time, I screwed up the left-rear speaker, which I only discovered after installation.  If you’re following my footsteps, do yourself a favor and use a multi-meter to verify the wiring connections before plugging it all in and closing up the trim panels.  Nothing like pulling everything apart all over again, especially a Daimler-era Chrysler that doesn’t belong to you.

So I had everything solidly connected.  I counted my blessings and connected the wiring harness at both ends.

Drama-free, the new unit slides in with a satisfying click.  Then comes reconnecting the battery, turning the key, and finding out if it worked.  The radio prompts for initial setup, so I consider it a success.  Some nervous budging got the panel back into place, and the whole installation actually looks pretty good, despite the radio being glossy and everything else being matte.

Now on to the other half: permanently replacing my own car’s torque strut.

Either the upper mounts are putting some odd pressure on the engine, or rolling the front onto raps somehow pushes the engine forward.  I might never know, unless I put the whole car on a lift, which would only happen in a shop or a wealthy friend’s house.  So with this in mind, I pull out the Harbor Freight cable come-along from the last job.   To keep the engine from lurching forward when the screws come loose, I preloaded some tension, to be released when the new part is in.

But here I come to a problem.  The new polyurethane mount is a different shape than the old one, so the come-along’s hook is in the way, prohibiting me from slotting the bolt in.  I would just have to take off the come-along, attach the front end of the mount, then hook the winch back up and tension the engine back into place.

Problem deux: Be it by manufacturing defect or bracket deformation from having to install so many of the same part, the new mount is too thick for the bracket.  Either way, no amount of Jeremy Clarkson-style hammering would wedge the wider end into either bracket, so some trimmings must be made.

Dad’s got a pile of files and rasps in his workshop, so selecting an appropriate one and hammering out the inner barrel, I figured I’d only need to take off a millimeter or two.  Of course, I had no way of knowing when I’d get to that point, so after a few minutes filing I did a test-fitting, and immediately went back to the workshop for more filing.

One last try got the larger end into the rear bracket (just).  So I had to pull it out of the bracket and attach the front end before winching it so the hook wouldn’t get in the way.  More hammering was needed as it was still a snug fit, but hammering is always better when it leads to results, Mister Clarkson.

Bolts in place, tension released, and one last check to make sure I hadn’t done anything stupid to something critical, I gave the engine a turn to check the mount’s effectiveness.

Here, we had something a bit strange.  There was more… “gusto” from the engine, I guess you could say.  Like a subwoofer was synced to the exhaust note of the car.  Stepping outside, I heard no difference.  I must assume that polyurethane is more resistant than rubber, and the mount is translating more engine vibrations to the chassis.  It might be annoying to someone more accustomed to the ride in a Lexus, but it suits me just fine.  Eddy just growls now.

Feels like I added 10% more horsepower without having to add any stickers! Now I’m wondering what I would get with a real performance part…

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